张斌,李滨阳,郝晓蕾,等. 氮气泡沫解除气井软堵塞技术及应用[J]. 石油钻采工艺,2025,47(4):472-480. DOI: 10.13639/j.odpt.202504001
引用本文: 张斌,李滨阳,郝晓蕾,等. 氮气泡沫解除气井软堵塞技术及应用[J]. 石油钻采工艺,2025,47(4):472-480. DOI: 10.13639/j.odpt.202504001
ZHANG Bin, LI Binyang, HAO Xiaolei, et al. Nitrogen foam technology for removing soft plugging in gas wells and its application[J]. Oil Drilling & Production Technology, 2025, 47(4): 472-480. DOI: 10.13639/j.odpt.202504001
Citation: ZHANG Bin, LI Binyang, HAO Xiaolei, et al. Nitrogen foam technology for removing soft plugging in gas wells and its application[J]. Oil Drilling & Production Technology, 2025, 47(4): 472-480. DOI: 10.13639/j.odpt.202504001

氮气泡沫解除气井软堵塞技术及应用

Nitrogen foam technology for removing soft plugging in gas wells and its application

  • 摘要: 气井生产中后期,生产管柱内普遍出现的“软堵塞”问题已成为制约产能的关键。这种堵塞主要由凝析油、油泥砂、泡排剂残留物等混合物在低流速条件下沉积形成。针对此问题提出了“软堵塞”的概念并揭示了其形成机理,进而指出了堵塞后的主要动态生产特征及危害,为识别此类气井提供了重要依据。在此基础上,基于氮气泡沫流体低密度和高携砂能力的特性,建立了“泡沫密度-排量”协同控制模型。通过优化冲洗参数实现了氮气泡沫携砂效率与储层保护之间的平衡。8口井(页岩气井6口、致密砂岩气井2口)的现场试验结果显示,该技术解堵成功率100%,单井增气量提升至原来的3.3倍,有效期达90 d以上。研究表明,氮气泡沫冲洗技术可为气井中后期稳产提供经济高效的解决方案,具有显著推广应用价值。

     

    Abstract: In the middle and later stages of gas well production, "soft plugging" issue that commonly occurs in the production string has become a key challenge restricting productivity. This kind of plugging is mainly formed by the deposition of a mixture of condensate oil, oil sludge sand, and residual foaming agents under low flow rate conditions. To address this problem, the concept of "soft plugging" is proposed, and its formation mechanism is revealed. And then, the main dynamic production behavior and hazards after plugging are identified, providing an important basis for recognizing such gas wells. Based on the low density and high sand-carrying capacity of nitrogen foam fluid, a "foam density - flow rate" cooperative control model is established. By optimizing the flushing parameters, a balance is achieved between the sand-carrying efficiency of nitrogen foam and reservoir protection. Field tests in 8 wells (6 shale gas wells and 2 tight sandstone gas wells) demonstrates a 100% success rate in removing plugging, the gas production of single well is increased by 3.3 times, and the validity exceeds 90 days. Research indicates that nitrogen foam flushing technology can provide an economical and efficient solution for the stable production of gas wells in the middle and later stages, with significant potential for broad application.

     

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