李集,卢运虎,韦世明,等. 塔里木盆地台盆区石炭系盐膏层套管损坏机理及防治对策[J]. 石油钻采工艺,2025,47(6):704-711. DOI: 10.13639/j.odpt.202508001
引用本文: 李集,卢运虎,韦世明,等. 塔里木盆地台盆区石炭系盐膏层套管损坏机理及防治对策[J]. 石油钻采工艺,2025,47(6):704-711. DOI: 10.13639/j.odpt.202508001
LI Ji, LU Yunhu, WEI Shiming, et al. Mechanism and countermeasures for casing failure in carboniferous salt-gypsum formation in the platform-basin transitional area, Tarim basin[J]. Oil Drilling & Production Technology, 2025, 47(6): 704-711. DOI: 10.13639/j.odpt.202508001
Citation: LI Ji, LU Yunhu, WEI Shiming, et al. Mechanism and countermeasures for casing failure in carboniferous salt-gypsum formation in the platform-basin transitional area, Tarim basin[J]. Oil Drilling & Production Technology, 2025, 47(6): 704-711. DOI: 10.13639/j.odpt.202508001

塔里木盆地台盆区石炭系盐膏层套管损坏机理及防治对策

Mechanism and countermeasures for casing failure in carboniferous salt-gypsum formation in the platform-basin transitional area, Tarim basin

  • 摘要: 塔里木盆地台盆区石炭系盐膏层钻井过程中频繁发生套管损坏事故,严重影响了钻井安全。为明确套损机理并制定有效防治策略,基于钻、测、录井资料,系统分析了典型套损案例,识别出盐膏层套损的关键控制因素,并建立了盐膏层套管损坏的力学模型。通过该模型,定量揭示了下部悬挂套管长度、井径扩大率和套管居中度等参数对套管安全系数的影响。研究发现:该区域套损机理为硬质泥岩支点-盐溶扩径-偏心载荷协同作用导致的套管弯曲失效。基于此,提出了三项针对性优化措施:优化井身结构,将二开中完井深延伸至盐膏层下界,并采用大尺寸高钢级套管封固盐膏层;调控钻井液性能控制盐岩溶解速率,降低井径扩大率,保障井眼规则性;下套管前进行通井作业,并在封盐套管上部安装扶正器,提高套管居中度。现场4口新井的应用结果表明,实施该套技术方案后,套损事故发生率降为0,显著提升了钻井作业的安全性和经济性。研究成果为深层盐膏层安全钻井提供了重要的理论支撑和技术指导。

     

    Abstract: Frequent casing failure incidents during drilling through the Carboniferous salt-gypsum formations in the platform-basin transitional area in the Tarim Basin have severely compromised drilling safety. To address the unclear mechanisms and lack of effective preventive measures for casing failure in this region, this study analyzed the characteristic patterns of typical casing failure cases based on drilling, logging, and mud logging data. Dominant factors for casing failure in salt-gypsum formations were identified, and a mechanical model was established for casing failures in such formations. This model was used to quantitatively assess the impact of parameters such as the lower suspended casing length, hole diameter enlargement rate, and casing centralization degree on casing safety factors. The research revealed that the casing failure mechanism in this area is the synergistic effect of hard mudstone pivot points, salt dissolution-induced hole enlargement, and eccentric loading, ultimately leading to casing buckling failure. Based on calculations from the mechanical model, three optimization measures were proposed: optimizing wellbore configuration by extending the intermediate casing setting depth of the second spud section to the lower boundary of the salt-gypsum formation and sealing the layer with large-diameter and high-strength casing; regulating drilling fluid properties to control salt rock dissolution rate, reduce hole diameter enlargement rate, and ensure wellbore regularity; and, performing reaming before running casing, and installing centralizers above the casing section sealing the salt formation to improve casing centralization degree. Field applications in four new wells demonstrated that implementing this technical solution reduced the casing failure incident rate to zero, significantly enhancing drilling safety and economic efficiency. The research findings provide crucial theoretical support and technical guidance for the safe drilling of deep salt-gypsum formations.

     

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