余世杰, 袁鹏斌, 魏立明, 刘贤文, 高健峰, 吕拴录. 钻杆接头螺纹粘扣原因分析[J]. 石油钻采工艺, 2011, 33(1): 112-116.
引用本文: 余世杰, 袁鹏斌, 魏立明, 刘贤文, 高健峰, 吕拴录. 钻杆接头螺纹粘扣原因分析[J]. 石油钻采工艺, 2011, 33(1): 112-116.
YU Shijie, YUAN Pengbin, WEI Liming, LIU Xianwen, GAO Jianfeng, LV Shuanlu. Cause analysis of drill pipe joint thread galling[J]. Oil Drilling & Production Technology, 2011, 33(1): 112-116.
Citation: YU Shijie, YUAN Pengbin, WEI Liming, LIU Xianwen, GAO Jianfeng, LV Shuanlu. Cause analysis of drill pipe joint thread galling[J]. Oil Drilling & Production Technology, 2011, 33(1): 112-116.

钻杆接头螺纹粘扣原因分析

Cause analysis of drill pipe joint thread galling

  • 摘要: 某油田先后出现多起钻杆接头螺纹粘扣事故,且都为新钻杆,给油田造成了较大的经济损失。为了避免此类事故的再次发生,结合现场调查,通过对钻杆粘扣的接头螺纹形貌进行宏观观察,及对接头材料的力学性能、化学成分、金相组织进行了全面的试验分析。结果表明,该次螺纹大面积粘扣与接头材质无关,而是井队在接立柱过程中,立柱中心轴线与入井钻杆轴线同心度偏差较大,在螺纹旋合时引起偏斜对扣,造成接头螺纹碰伤,以及高速引扣,引起公母螺纹牙齿相互干涉,造成螺纹面的挤压磨损,塑性变形,最终导致大面积的接头粘扣。最后根据失效原因,提出了相对应的改进措施和建议。

     

    Abstract: A number of drill pipe joint thread-galling failures were discovered in the oil field mentioned, and all of them happened on new pipes, which brings a big loss to oil field economy. Field survey was applied to the failure accident. Mechanical properties test, chemical composition analysis, and micro-structure examination to the joint material and the macro-appearance observation to the tool joint threads were taken. The results showed that, as there was a great central axis deviation of the stands in picking-up process, which caused mechanical damage to the joint threads when make-up, and as the guiding process to make-up was in high speed, the thread galling of tool joints happened eventually. In the end, the prevention methods and suggestions were put forward based on the failure cause.

     

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